Yesterday I took, what I hope to be, my last walk across Pleasure Beach Island in Bridgeport, Connecticut. The task at hand was repairing the antenna array for WICC. There turned out to be several issues that were addressed in turn.
WICC tower feed point, courtesy of NECRAT
The trouble started when the feed line between the ATU and the tower became disconnected during a storm. That consists of a 1-inch copper pipe extending from the ATU feed through an insulator up to a brass plate suspended between the four tower legs by hard-drawn single 0 copper wire. The feed line separated at the brass plate which, unfortunately, is approximately eighteen feet in the air.
North Tower feed point connection, cold soldered
The feed line was repaired, but not effectively. By the looks of the picture, the brass plate never got hot enough to accept the solder.
After the feed line was re-repaired, other issues became apparent. The base impedance of the tower was still off and the array was still way out of tolerance.
It was noticed that several bypass capacitors on both of the tower lighting chokes were blown open. Those were replaced and the tower lighting chokes were checked for shorted turns. While it is always nice to replace burned-out parts, this did not correct the problem.
Finally, we were back at the base of the tower with the defective feed point and a decision to grab the pipe and give it a good shake to see if it came apart again. It did not, but then I realized that that tower was supposed to be back in the circuit and I did not receive any RF burns for my carelessness.
We dug into the ATU and discovered that the input capacitor was marginal and there was a large crack in it. The output capacitor seemed to be completely open. The base current that we were seeing on the base current meter was being induced by the other tower. It all began to make sense.
Bad Capacitor
The parts were ordered and shipped and I made another trip out to install them myself.
Thus, on this particular day, I had my tool bag, an OIB-3 with fresh batteries, my cordless drill, drill bits, and three type 294 mica capacitors. I took the drill because the new capacitors were quite a bit larger than the old ones, so I needed to move the stand-off insulators to remount them.
Pleasure Beach pier, foggy day
The walk from the end of the dock to the transmitter site is approximately 900 meters or 0.55 miles, according to google maps. On a nice day, it is a pleasant walk. On not-so-nice days, it can be less so. It was foggy with light drizzle. Not enough to get wet right away, but enough to get slowly soaked while working on the ATU repairs.
WICC square base self-supporting towers, manufactured by Milliken Tower, circa 1928
With the new capacitors installed, I needed to adjust the array back into tolerance, which didn’t take too long. I made a short video of the station running at full power showing the antenna monitor readings for both the day and night patterns. Then packed up and headed back to the dock.
My ride is here
I wanted to take a set of monitor points, but the FIM-41 had been moved to another location. That was fine, I was getting pretty uncomfortable in my wet clothes, so I headed home.
I do not know what the record is for the longest tube life, however, this particular tube lasted 17 years, 11 months, and 23 days. That’s 157,596 hours.
This was installed new in a Broadcast Electronics FM20T transmitter which was placed online on June 6, 2001. It lasted until May 28th, 2019 with almost no downtime. Towards the end, the emissions started dropping off and we increased the filament voltage up to 10 volts. When you have to increase the filament voltage, that really is the end for a tube.
The new tube was put in and I carefully marked out the date in the maintenance log. The hour meter on the transmitter stopped working several years ago.
Prior to this, the longest tube life I’d experienced was an EEV 4CX35000C from an MW-50B transmitter RF section. When that tube came out, it looked like it have been on fire.
I have been remiss in updating this thing, even for Christmas and the New Year. It has been a busy time, but also, it seems that there is nothing exciting to write about. Continuing on writing about another transmitter installation or studio project seems redundant.
That being said, I have moved into the realm of high quality audio. I miss that days when a good audio was the general rule, in both home audio and broadcast. People have become used to crappy .mp3s played through crappy computer speakers or cheap ear buds.
Knowing just enough to be dangerous, I figured I should do a little bit of research before spending a lot of money foolishly. I discovered that there are gobs and gobs of information on various forums and other places around the intertubes. Most of it seems to be good, although one has to be careful and backup whatever is out there with science. There are several books about DIY speaker building, amplifier construction, turntable maintenance, etc. Picking the thing that I thought would be easiest and lead to the biggest improvement in my own audio system, I set out to build a pair of speakers.
Most people probably don’t realize this, but there is quite a bit of work that goes into a well designed pair of speakers. I began by thinking about what the end use will be, which eventually is a single ended tube amp based on a KT88 design. As such, I figured the efficiency of the drivers was an important detail. Power handling capability of the driver could be quite low, 30-50 watts or so. Searching through several speaker manufacture’s web sites, I found a small sized, full range driver that is fairly efficient and has excellent reviews.
The Tang Band W4-1337SDF has a published sensitivity of 89dB/1 watt/1 meter. Its frequency response is 70-20,000 Hz. It also has a titanium speaker cone. There have been many an article written and much ink spilled on metal cone speakers, so I did not quite know what to think of the titanium cone. I did spend a goodly amount of time reading all of the reviews on this particular driver and decided to take the risk and buy two of them.
Next step was to calculate the proper interior volume of the speaker enclosure for a vented box. Vented or ported speaker enclosures are generally more efficient than sealed units. Vented boxes are a little bit more exacting to build correctly. Again, lots of information available on line, some of it is good. In the end, I downloaded a free software package called WinISD.
WinISD takes into account all of the Thiele/Small characteristics of the driver and generates a basic box design. I looked at the proposed box and decided that the internal volume was the important part, the actual shape of the box is secondary so long as it is not an exact cube. Instead of the 2:3 ratio rectangle, I choose something different; a 1:4 rectangle.
Making cuts for speaker boxes
Next, I began looking around at available materials. I have plenty of wood laying around from previous projects, so I decided to make the boxes from 1×6 clear pine. This is also contrary to conventional wisdom, as MDF is the preferred choice in speaker cabinets. This is because natural wood has a resonate frequency, which can create problems. As these are low power units, I figured, if it was a huge problem I could always make another cabinet out of MDF. In the mean time, the wood, glue, paint, screws, foam insulation, tung oil finish where already in the shop. Why buy more stuff?
I also wanted to add a tweeter (Peerless D19TD-05) to cover the high end and a simple 1 pole (or first order) cross over.
Speaker box work
Thus, parts ordered, I started working on the boxes. I decided that rabbit joints where a better choice than mitered 45 degree joints. I used the router table to make the joints, cutouts and round the cabinet edges. During the sanding process, I discovered that the wood boxes do indeed resonate somewhere around the 300 to 400 Hz region. More on that later.
Speaker box glue up
The fronts and backs are made out of 1/2 inch plywood, painted flat black. There is a one inch rear firing port. The box itself is larger than what is called for. I made it thus because there where a couple of different recommendations on box volume and I wanted to add some cross bracing, which takes up space.
Speaker box, foam dampening and bracing
I thought about ways to dampen the wood box resonance and came up with a bit of rigid foam insulation, again left over from some long ago renovation project. My idea was to take up some of that excess internal volume, but they might also work to dampen the resonance. I cut several pieces of this material so that they fit snugly into the box. I then used the sander to resonate the box and see what effect the foam insulation was having. In the end, I came up one piece at the top and bottom and one approximately in the middle. Once I was happy, these were glued in place. This significantly dampened the resonance. I also added quite a bit of acoustical foam inside the box.
First order crossover
The cross over is designed for 4000 Hz. It consists of a 5 uF capacitor and a .31 uH inductor. I am a minimalist at heart. I thought about nixing the inductor altogether, but I think running both the driver and tweeter at the same time would lower the impedance too much over the high frequencies.
Completed speakers
The completed project was bench tested using a software program called DATS:
Speaker impedance sweep
The Tang Band driver is resonant at 60 Hz or so. After the F3 frequency, calculated to be 101 Hz, the impedance looks good all the way out to 20 KHz. It appears the F3 frequency is slightly higher, likely because the port is too short.
I messed around with the internal box volume by adding and taking away pieces of foam insulation. In the end, I found that the original volume calculated by WinISD worked (and sounded) the best.
I set these up and took a listen. Using a reference recording of Tschaikovsky (piano concert #1, B flat minor) I found these speakers sound excellent. The stringed instruments and horns in particular sound very detailed. The piano is open and natural. If I close my eyes, it sounds like it is right in front of me. Perhaps that is the wood box. I tried them on several different types of music; jazz, rock and even Tom’s Dinner. It may be a bit biased, however, I find these speakers to be far and above anything else I have owned in the past. They sound great.
My only very minor gripe is the bass is not as responsive as I would like. The low end starts around 90 Hz. This showed up in the F3 frequency reported by WinISD. I have a Polk Audio subwoofer that I am using (temporarily) to add the bass back into the mix. I could also try tuning the ports a little bit to move the F3 down. That may also require removing some if the foam from the box to increase the internal volume.
I also made a small mistake when cutting the wood for the box, as they are slightly too narrow and the driver does not fully fit onto the plywood front. That is because I started working on this before I had the drivers in hand. If I make another pair, I’ll make the cabinet a little bit wider.
Speaker frequency room response
I also ran a couple of sweeps with Room EQ Wizard. That 300-400 Hz box resonance shows up in the sweep, but it is not noticeable when listening. Without the subwoofer turned on, the bass does not start to pick up until about 70 Hz or so, which exactly the spec on the driver. Funny how that works.
Speaker and subwoofer frequency response
This is with the subwoofer turned on. Notice the little hum around 40 Hz, that is the hallway to the bathroom acting as a bass resonator. Unfortunately, my listening room has some uncurable defects; I cannot get rid of the hallway to the bathroom because eventually that room comes in handy. I need to get some acoustical material up on the wall and perhaps the ceiling. I was thinking of a Helmholtz resonator in the wall.
Speakers mounted
They sound slightly better if they are moved off axis from the back wall.
My total cost was about $180.00, not counting the materials I already had on hand. After listening to these for several days, I can say they stack up well against speakers that cost ten times what I paid.
Next project; the matching subwoofer. I have some ideas…
After a bit of reflection and a few good conversations over the New Year’s Holiday, I decided that I should continue my work on this blog. I would like to thank all those that have stuck by and waited. I have received numerous emails and messages offline, all of which have been read and appreciated.
Since the abrupt stoppage last July, which was absolutely necessary for me, many things have happened within the business. Fortunately, during the hiatus, I was still taking pictures. After sorting through them, here are a few interesting things that happened:
WROW-AM Steel mounting poles on antenna array field
This project required many steel mounting posts to be driven into the ground around the AM towers. I don’t even know how many, but I would hazard a guess of over three hundred. Each one of those mounting posts was hand-dug down a depth of 6-10 inches to look for ground wires. Where ever a ground wire was found, it was moved out of the way before the post was set.
WROW-AM ground wire moved out of way
Basically, the solar array covers about 1/2 of the antenna array field. All of the steel mounting hardware is tied into the ground system, making, what I am sure is a pretty large above-ground counterpoise.
WROW-AM solar panel mounting hardware
View from the south looking north:
Solar Array installed on WROW antenna array, Glenmont, NY
View from the north, outside of the transmitter building, looking south:
Solar Array installed on WROW antenna array, Glenmont, NY
Power company interface and disconnect:
Solar Array utility company disconnect, Glenmont, NY
The utility company had to upgrade the transmission lines to the nearest substation to handle the additional power produced by the solar system. All in all, it was a fun project to watch happen.
At a certain studio building, which is over 150 years old, the roof needed to be replaced. This required that the 3.2-meter satellite dish and non-penetrating roof mount be moved out of the way while that section of the roof was worked on.
3.2 meter satellite dish
Dish was ready to move, and all of the concrete ballast was removed and taken down from the roof. The roofing contractors constructed a caddy and the entire dish and mount were slid forward onto the area in front of it. Since the front part of the roof was not reinforced to hold up the satellite dish, we did not ballast the mount and the XDS receivers ran off of the streaming audio for a couple of days until the dish was put back in its original position.
3.2 meter satellite dish ready to move
A couple of other studio projects have been underway in various places. Pictures to follow…
One of our clients sold their radio stations to another one of our clients.
There has also been a bankruptcy of a major radio company here in the good ol’ US of A. Something that was not unexpected, however, the ramifications of which are still being decided on in various board rooms. One of the issues as contractors is whether or not we will get paid for our work. All things considered, it could be much worse.
Learned a valuable lesson about mice chewed wires on generator battery chargers. I noticed that the battery charger seemed to be dead, therefore, I reached down to make sure the AC plug was in all the way. A loud pop and flash followed and this was the result:
Arc burns, right hand
My hand felt a bit warm for a while. The fourth digit suffered some minor burns. There is at least one guy I know that would be threatening a lawsuit right now. Me, not so much… All of the high voltage stuff we work on; power supplies that can go to 25 KV, and a simple 120 VAC plug is the thing that gets me.
The return of the rotary phase maker.
Rotary phase maker, Kay Industries T-10000-A
Mechanically derived 3rd phase used when the old tube type transmitter cannot be converted to single phase service.
Those are just a few of the things I have been working on. I will generate some posts on current projects underway. Those projects include a 2 KW FM transmitter installation, another studio project, repair work on a Harris Z16HD transmitter, etc