Ten years on

It was ten years ago that I registered the domain name for Engineering Radio. A few days later, I put the first post up. It is still there.  Those were different times for me personally and the business in general.  There certainly have been trials, but it has never been dull.

Periodically, I go back through the posts and delete anything that is no longer relevant.  I would estimate about 1/4 to 1/3 of the content has been deleted over the years.  It is a good exercise to go back through and read what I wrote previously.

Currently, the stats are:

  • 787 published posts, there are a few in the wings waiting to be finished
  • 4459 comments
  • Approximately 200 page views per day
  • 170 RSS feed subscriptions

I lost the country counter, but I believe the split is still about 60/40 US readers vs other countries.

I will continue on with this thing for as long as I feel it is worthwhile.

Last Walk across The Island

Yesterday I took, what I hope to be, my last walk across Pleasure Beach Island in Bridgeport, Connecticut. The task at hand was repairing the antenna array for WICC. There turned out to be several issues that were addressed in turn.

WICC tower feed point, courtesy of NECRAT

The trouble started when the feed line between the ATU and the tower became disconnected during a storm. That consists of a 1-inch copper pipe extending from the ATU feed through an insulator up to a brass plate suspended between the four tower legs by hard-drawn single 0 copper wire. The feed line separated at the brass plate which, unfortunately, is approximately eighteen feet in the air.

North Tower feed point connection, cold soldered

The feed line was repaired, but not effectively. By the looks of the picture, the brass plate never got hot enough to accept the solder.

After the feed line was re-repaired, other issues became apparent. The base impedance of the tower was still off and the array was still way out of tolerance.

It was noticed that several bypass capacitors on both of the tower lighting chokes were blown open. Those were replaced and the tower lighting chokes were checked for shorted turns. While it is always nice to replace burned-out parts, this did not correct the problem.

Finally, we were back at the base of the tower with the defective feed point and a decision to grab the pipe and give it a good shake to see if it came apart again. It did not, but then I realized that that tower was supposed to be back in the circuit and I did not receive any RF burns for my carelessness.

We dug into the ATU and discovered that the input capacitor was marginal and there was a large crack in it. The output capacitor seemed to be completely open. The base current that we were seeing on the base current meter was being induced by the other tower. It all began to make sense.

Bad Capacitor

The parts were ordered and shipped and I made another trip out to install them myself.

Thus, on this particular day, I had my tool bag, an OIB-3 with fresh batteries, my cordless drill, drill bits, and three type 294 mica capacitors. I took the drill because the new capacitors were quite a bit larger than the old ones, so I needed to move the stand-off insulators to remount them.

Pleasure Beach pier, foggy day

The walk from the end of the dock to the transmitter site is approximately 900 meters or 0.55 miles, according to google maps. On a nice day, it is a pleasant walk. On not-so-nice days, it can be less so. It was foggy with light drizzle. Not enough to get wet right away, but enough to get slowly soaked while working on the ATU repairs.

WICC square base self-supporting towers, manufactured by Milliken Tower, circa 1928

With the new capacitors installed, I needed to adjust the array back into tolerance, which didn’t take too long. I made a short video of the station running at full power showing the antenna monitor readings for both the day and night patterns. Then packed up and headed back to the dock.

My ride is here

I wanted to take a set of monitor points, but the FIM-41 had been moved to another location. That was fine, I was getting pretty uncomfortable in my wet clothes, so I headed home.

Goodbye, WICC.

Almost Eighteen Years

I do not know what the record is for the longest tube life, however, this particular tube lasted 17 years, 11 months, and 23 days.  That’s 157,596 hours.

I had written about this almost five years ago: https://www.engineeringradio.us/blog/2014/12/longest-tube-life/

The last one was last fall: https://www.engineeringradio.us/blog/2018/09/i-almost-hate-to-say-anything-but/

Eimac 4CX12000A power tube, serial number RHH108

This was installed new in a Broadcast Electronics FM20T transmitter which was placed online on June 6, 2001.  It lasted until May 28th, 2019 with almost no downtime.  Towards the end, the emissions started dropping off and we increased the filament voltage up to 10 volts.  When you have to increase the filament voltage, that really is the end for a tube.

The new tube was put in and I carefully marked out the date in the maintenance log.  The hour meter on the transmitter stopped working several years ago.

Prior to this, the longest tube life I’d experienced was an EEV 4CX35000C from an MW-50B transmitter RF section.  When that tube came out, it looked like it have been on fire.

Box One

I have been remiss in updating this thing, even for Christmas and the New Year.  It has been a busy time, but also, it seems that there is nothing exciting to write about.  Continuing on writing about another transmitter installation or studio project seems redundant.

That being said, I have moved into the realm of high quality audio.  I miss that days when a good audio was the general rule, in both home audio and broadcast.  People have become used to crappy .mp3s played through crappy computer speakers or cheap ear buds.

Knowing just enough to be dangerous, I figured I should do a little bit of research before spending a lot of money foolishly.  I discovered that there are gobs and gobs of information on various forums and other places around the intertubes.  Most of it seems to be good, although one has to be careful and backup whatever is out there with science.  There are several books about DIY speaker building, amplifier construction, turntable maintenance, etc.  Picking the thing that I thought would be easiest and lead to the  biggest improvement in my own audio system, I set out to build a pair of speakers.

Most people probably don’t realize this, but there is quite a bit of work that goes into a well designed pair of speakers.  I began by thinking about what the end use will be, which eventually is a single ended tube amp based on a KT88 design.  As such, I figured the efficiency of the drivers was an important detail.  Power handling capability of the driver could be quite low, 30-50 watts or so.  Searching through several speaker manufacture’s web sites, I found a small sized, full range driver that is fairly efficient and has excellent reviews.

The Tang Band W4-1337SDF has a published sensitivity of 89dB/1 watt/1 meter.  Its frequency response is 70-20,000 Hz.  It also has a titanium speaker cone.  There have been many an article written and much ink spilled on metal cone speakers, so I did not quite know what to think of the titanium cone.  I did spend a goodly amount of time reading all of the reviews on this particular driver and decided to take the risk and buy two of them.

Next step was to calculate the proper interior volume of the speaker enclosure for a vented box.  Vented or ported speaker enclosures are generally more efficient than sealed units.  Vented boxes are a little bit more exacting to build correctly.  Again, lots of information available on line, some of it is good.  In the end, I downloaded a free software package called WinISD.

WinISD takes into account all of the Thiele/Small characteristics of the driver and generates  a basic box design.  I looked at the proposed box and decided that the internal volume was the important part, the actual shape of the box is secondary so long as it is not an exact cube.  Instead of the 2:3 ratio rectangle, I choose something different; a 1:4 rectangle.

Making cuts for speaker boxes
Making cuts for speaker boxes

Next, I began looking around at available materials.  I have plenty of wood laying around from previous projects, so I decided to make the boxes from 1×6 clear pine.  This is also contrary to conventional wisdom, as MDF is the preferred choice in speaker cabinets.  This is because natural wood has a resonate frequency, which can create problems.  As these are low power units, I figured, if it was a huge problem I could always make another cabinet out of MDF.  In the mean time, the wood, glue, paint, screws, foam insulation, tung oil finish where already in the shop.  Why buy more stuff?

I also wanted to add a tweeter (Peerless D19TD-05) to cover the high end and a simple 1 pole (or first order) cross over.

Speaker box work
Speaker box work

Thus, parts ordered, I started working on the boxes.  I decided that rabbit joints where a better choice than mitered 45 degree joints.  I used the router table to make the joints, cutouts and round the cabinet edges.  During the sanding process, I discovered that the wood boxes do indeed resonate somewhere around the 300 to 400 Hz region.  More on that later.

Speaker box glue up
Speaker box glue up

The fronts and backs are made out of 1/2 inch plywood, painted flat black.  There is a one inch rear firing port.  The box itself is larger than what is called for.  I made it thus because there where a couple of different recommendations on box volume and I wanted to add some cross bracing, which takes up space.

Speaker box, foam dampening and bracing
Speaker box, foam dampening and bracing

I thought about ways to dampen the wood box resonance and came up with a bit of rigid foam insulation, again left over from some long ago renovation project.  My idea was to take up some of that excess internal volume, but they might also work to dampen the resonance.  I cut several pieces of this material so that they fit snugly into the box.  I then used the sander to resonate the box and see what effect the foam insulation was having.  In the end, I came up one piece at the top and bottom and one approximately in the middle.  Once I was happy, these were glued in place.  This significantly dampened the resonance.  I also added quite a bit of acoustical foam inside the box.

First order crossover
First order crossover

The cross over is designed for 4000 Hz.  It consists of a 5 uF capacitor and a .31 uH inductor.  I am a minimalist at heart.  I thought about nixing the inductor altogether, but I think running both the driver and tweeter at the same time would lower the impedance too much over the high frequencies.

Completed speakers
Completed speakers

The completed project was bench tested using a software program called DATS:

Speaker impedance sweep
Speaker impedance sweep

The Tang Band driver is resonant at 60 Hz or so.  After the F3 frequency, calculated to be 101 Hz, the impedance looks good all the way out to 20 KHz.  It appears the F3 frequency is slightly higher, likely because the port is too short.

I messed around with the internal box volume by adding and taking away pieces of foam insulation.  In the end, I found that the original volume calculated by WinISD worked (and sounded) the best.

I set these up and took a listen.  Using a reference recording of Tschaikovsky (piano concert #1, B flat minor) I found these speakers sound excellent.  The stringed instruments and horns in particular sound very detailed.  The piano is open and natural.  If I close my eyes, it sounds like it is right in front of me.  Perhaps that is the wood box.  I tried them on several different types of music; jazz, rock and even Tom’s Dinner.  It may be a bit biased, however, I find these speakers to be far and above anything else I have owned in the past.  They sound great.

My only very minor gripe is the bass is not as responsive as I would like.  The low end starts around 90 Hz.  This showed up in the F3 frequency reported by WinISD.  I have a Polk Audio subwoofer that I am using (temporarily) to add the bass back into the mix.  I could also try tuning the ports a little bit to move the F3 down.  That may also require removing some if the foam from the box to increase the internal volume.

I also made a small mistake when cutting the wood for the box, as they are slightly too narrow and the driver does not fully fit onto the plywood front.  That is because I started working on this before I had the drivers in hand.  If I make another pair, I’ll make the cabinet a little bit wider.

Speaker frequency room response
Speaker frequency room response

I also ran a couple of sweeps with Room EQ Wizard.  That 300-400 Hz box resonance shows up in the sweep, but it is not noticeable when listening.  Without the subwoofer turned on, the bass does not start to pick up until about 70 Hz or so, which exactly the spec on the driver.  Funny how that works.

Speaker and subwoofer
Speaker and subwoofer frequency response

This is with the subwoofer turned on. Notice the little hum around 40 Hz, that is the hallway to the bathroom acting as a bass resonator.  Unfortunately, my listening room has some uncurable defects; I cannot get rid of the hallway to the bathroom because eventually that room comes in handy.  I need to get some acoustical material up on the wall and perhaps the ceiling.  I was thinking of a Helmholtz resonator in the wall.

Speakers mounted
Speakers mounted

They sound slightly better if they are moved off axis from the back wall.

My total cost was about $180.00, not counting the materials I already had on hand.  After listening to these for several days, I can say they stack up well against speakers that cost ten times what I paid.

Next project; the matching subwoofer.  I have some ideas…