That saying originates from Greek and Roman times, when Sirius, the Dog Star, aligned with the Sun during July and August and was thought to bring extra heat to the earth. The Dog Days are evil times; seas boil, wine turns sour, dogs grow mad, and all other creatures became languid; causing to man, among other diseases, burning fevers, hysterics, and phrensies.
Bad news, indeed. Add to that; air conditioners fail, general managers become cranky, and transmitters overheat causing damage to sensitive control circuits, which is even worse.
We shall be busy dealing with things like this:
Air conditioning condenser with low refrigerant. This unit either has a leak or was not charged properly. I would hazard the former.
Fan blade on condenser coil failed due to metal fatigue. I have seen this in more than one place.
These wall-mount Bard AC units are pretty reliable, however, even they fail from time to time. The best course of action is to have a maintenance plan, a backup plan, and the number of the best HVAC contractor that can be found.
It was a hot day, it was a cold day. The tube transmitter was running, the solid-state (HD-1) transmitter was off the air. The books show that the company has deep pockets, but the accountant has short arms. And so it goes. In a sordid, yet familiar tale of leaping three-quarters of the way across a river, the builders of this transmitter site seemed to think of everything except the cooling requirements for a 35 KW FM transmitter.
Instead of installing real commercial AC units, someone decided that 34,000 BTU window units were the way to go. At one time, there were eight of those units, all single phase 240 volts sucking down gobs of power and freezing up when the outside temperature dropped below 40°F. This was always a problem but became more so when we took over the maintenance of this site. When there was a full-time engineer, his time, apparently, could be wasted running back and forth turning the window units on or off in the winter as required. Now that a contract company is doing the work, it becomes cost prohibitive to require such things.
Therefore, the time had come to make a change. To that end, six of the 34,000 BTU window units were removed from the building. Two of the existing holes in the wall were used to create an emergency cooling system, consisting of a 4,292 CFM fan and a couple of shutters. Two other holes were used for the new air conditioners and two holes were blocked up. The remaining two window units were left in place in the combiner room, which is a separate cooling zone.
The new ACs are five-ton wall-mount Bard units. These are three phase and should be more than enough to keep the transmitters cool. Here is how I arrived at that conclusion:
The entire building load when the main transmitter is running at full power, without the transmitter room air conditioning, is 60 KW.
All of the building loads except the transmitters go through a single-phase panel.
The load on the single phase panel is 10 KW, thus the transmitter load is 50 KW (this 10 KW is mostly the single phase AC units in the combiner room)
The TPO is 32 KW, therefore the transmitter is generating 18 KW of waste heat.
One watt-hour = 3.412 BTU of energy, thus
18,000-watt-hours equals 61,416 BTUs
One ton = 12,000 BTU, thus
61,416 BTU ÷ 12,000 BTU = 5.118 tons
That will take care of the main transmitter waste heat. The HD transmitter generates another 4,000 watts of waste heat or 1.37 tons. The combiner is in another room and doesn’t factor into the calculation. The rest of the equipment is inconsequential, adding up to less than 100 watts.
The solar gain is more difficult to calculate, as it is based on the building structure, the type of construction, and the heat gain (loss) through the walls and doors. This building is concrete block, insulated, and has no windows. It is unshaded, however, it is painted a light color. All in all, the solar gain should be less than two tons on a hot day. Therefore the total AC load should be 8.25 tons or less.
All that is left now was to install the things. Just pull up the truck and use a crane to lift them in place, except, no; that plan won’t work. This is the transmitter site at the power plant and the 138 KV lines overhead precluded any lifting with a crane. We instead had to build ramps and move things around on large-hand trucks. One unit is installed on the rear of the building, the other on the front. It required several days to make the ramps and four people to muscle the things into place.
The bottom air intake holes needed to be cut out for the new units. Cutting into the concrete block while the BE FM 35A was running proved to be another challenge. We used several sheets of plastic, shop vacs, and extra air filters on the transmitters to keep the concrete dust out of the PA cavities and motor bearings.
Plan B cooling consists of a 4,292 CFM Venturi fan mounted on the rear wall of the building. The fan is controlled by a ceiling-mounted thermostat set to 95 degrees. If the AC’s fail, the ceiling temperature will rise and the fan will turn on.
The room volume is about 3600 cubic feet, therefore this fan will change the room air about once every 60 seconds or so. It is not the best plan to move humid, potentially dirty outside air through a building, but it it keeps the station on the air while the main AC units are being repaired, then so be it.
The entire system went on line last week and is working well.
Back in the day, when tube transmitters ruled the broadcast world, the common practice was to have a big cooling fan moving outside air through the transmitter building connected to a thermostat. Temperature swings of 30 to 40 degrees were common, however, the tube rigs could handle almost any temperature that didn’t melt plastic or freeze water.
Today’s solid-state transmitters are not that rugged. They like to have their rooms around 70 degrees +/- 10 degrees or so. Not to mention the other computer-controlled equipment commonly found at a transmitter site. Things like air chain processors, STLs, remote controls, etc. So, lots of air conditioning is the norm, and with lots of air conditioning comes lots of maintenance.
Air handler air filters need to be checked and replaced often. Condenser coils seem to attract every type of flying debris on the planet and need to be cleaned once, possibly twice per year depending on tree and weed species near the site. Even with preventative maintenance, occasionally things like this happen:
Of course, the entire cooling coil inside is frozen solid.
This condenser is low on refrigerant, causing icing problems. It has a slow leak somewhere and is about to be replaced. Other reasons for this happening are malfunctioning or non-existent low ambient kit on the condenser fan. Sometimes less than knowledgeable persons will install a 5-ton unit designed to run throughout the year but not take into account the effect of moving below-freezing air at high speed across the coils. Insufficient air moving across the cooling coil will also cause this. Insufficient airflow can be due to plugged air filters or clogged fan/blower blades.
This one is even better (same condenser unit):
The fan blade is sheared off and jammed into the condenser coil. This happened during power transfer from generator power to commercial power. Naturally, it was at 1 a.m. in the morning after a pole-mounted transformer had been replaced. When the building transferred back to commercial power, I went outside to use the “bathroom” before my two-hour drive back home. I thought I smelled something hot, you know that cooked paint/plastic smell, but couldn’t really track it down… the winds were kicking up and another thunderstorm was on the way.
The next afternoon, however, when the sun was up and the site was working on one air conditioner, the temperature alarm went off. Upon arrival, I found the condenser breaker tripped, resetting it caused the building lights to dim. The fan motor was shorted to the case. I would theorize the aluminum fan blade suffered from metal fatigue, likely because the blades were not balanced causing a vibration. When the power transfer occurred, there was just the right combination of torque and centripetal force to cause the blade to rip, and then lodge in the condenser coil.
The fan motor has been replaced, but I think it is time to replace the whole condenser unit, which will be expensive.
I found having a set of gauges to check the head pressure and suction is a good diagnostic tool to quickly pinpoint problems with HVAC units. This way, when the HVAC tech shows up, you can quickly point him in the right direction.
This is yet another addition of the “Burned up Sh*t” collection:
It is a breaker from a 5-ton AC compressor. Back in the bad old days when I was the Director of Engineering for a 28-station group Headquartered in Harrisburg, PA, I received a phone call from one of the local engineers. He stated that the studio AC unit compressor had burned out again and the breaker kept tripping. What did I think, asked him. I thought perhaps he should dig a little deeper and determine why the breaker was tripping before throwing another AC compressor at it. When are you coming to town again, he cheerfully inquired.
Okay, I get it.
I started by calling the HVAC company to inquire what had gone wrong with the compressors. Winding shorted to the case for both units was the answer received. It being July and mighty hot out, the various worker bees in the studio were feeling inconvenienced by the sweat in their eyes and dripping on their work, etc. I called the local manager and asked for a hotel room, I’d be up tomorrow. Then I called the HVAC guy back and asked in to meet me at the studio tomorrow afternoon.
Upon arrival the next morning, I found the fifth-floor studios to be hot, as reported. I trip to the roof location proved to be hotter still. I tested the voltages at the compressor unit with a DVM and everything looked good. A trip down to the utility room found the electrical panel in reasonable shape. Then the local engineering guy chimed in, “Oh yeah, I forgot to tell you, the breaker hums and gets hot when the compressor is on.”
It’s always that little bit of missing information…
I took the breaker out and sure enough, the fingers were all arched and nasty-looking.
I replaced the breaker, the HVAC guy showed up, with a new compressor and the studios began to cool off around 3 p.m.
Since then, I have specified Square D QO bolt-on breakers for new installations, especially for heavy loads like AC units, transmitters, and so on. They are a little more expensive, but in light of two AC compressors, the unscheduled trip out of town, and the grumbling staff, it is better to pay upfront for better equipment than to put up with preventable outages.