The AM Receiver problem

The technical problems with AM broadcasting can be broken down into three broad categories:

  • Interference from other AM stations
  • Interference from unintentional radiators (AKA electrical noise)
  • Poor receivers

Much of the poor fidelity issues with AM broadcast audio come from the narrow IF bandwidth of the typical AM receiver.  Older AM receivers had much wider IF bandwidths, sometimes as much as 15 KHz +/- carrier.  As the AM band was overfilled with stations starting in the late 1940s, this became a big problem.  The tube-type front ends with great sensitivity but not very much selectivity was unable to cope with adjacent channel interference, leading to what was known as “monkey chatter.” This type of interference can be technically described as the higher audio frequency peaks from adjacent channel stations being demodulated.  Those hearing this type of interference found it very annoying and rightly so.  Thus, receiver manufacturers were deluged with complaints about the poor quality of their units.  The solution was simple; narrow the bandwidth until the “monkey chatter” disappeared.  This new de facto standard IF bandwidth turned out to be +/- 3 KHz carrier.

It does not take a rocket scientist to see that 3 KHz audio is slightly better than telephone quality.  This was the beginning of the perceived AM low fidelity problem.  In the meantime, FM broadcasting, after years of lagging behind in spite of its superior audio, made great strides into mainstream acceptance.

NRSC-1 was supposed to reduce this type of interference by limiting AM broadcasting stations’ audio bandwidth to 10 KHz.  The idea was to attempt to keep the modulation index somewhat within the allotted channel.  This standard was mandated by the FCC in 1989, after which receiver manufacturers were to change their design to allow for broader IF bandwidths, thus improving AM fidelity.  There was even an AMAX standard adopted by some receiver manufacturers.  Unfortunately, by this time, the majority of AM stations were transitioning from music to talk radio.  The new standards were too little much too late.

A quick scan with a quality AM receiver shows that many stations are transmitting high-quality audio, which, with a properly adjusted IF bandwidth can sound remarkably good:

Screen shot - WEOK true oldies channel
Screen shot – WEOK True Oldies Channel

This is a screenshot from an SDR (Software Defined Radio) showing WEOK, Poughkeepsie, NY broadcasting the True Oldies Channel.  The signal strength is slightly low, but this is a rural area and the noise floor is also low.  I limited the bandwidth to +/- 7.5 KHz carrier because of the pre-emphasis used on most AM stations makes the high-end sound strident.  Looking at the spectral display, there is more audio available beyond what I am listening to.  This brings me to this; AM fidelity is not inherently inferior, it can sound quite good.  There is no reason why AM receiver manufacturers cannot improve their products to include some advanced features;

  • Variable IF bandwidth based on signal strength
  • Variable user selected IF bandwidth
  • Sharp selectivity – adjacent channel rejection
  • Selectable sideband demodulation (carrier plus upper or carrier plus lower sideband)

While this will never sound as good as FM stereo, it still can sound pretty good, especially with older music recorded before say 1975 or so.

Manufacturers would have to have some impetus to include these features in their chipsets, such as multiple requests by listeners who are looking for better AM quality, which leads us back to programming…

The other issues with AM electrical noise reception and interference from other radio stations are surmountable, so long as there is a reason to.  This, leads us back to… programming.

Repairing a computer monitor

I have seen many a Dell LCD computer monitor go south for want of a $0.50 part. Dell must have gotten a hold of a bad batch of capacitors because almost invariably, the problem is with the power supply capacitors for the backlight. The symptoms are; the monitor goes very dim and can only be read when shining a light on it, or the power button flashes green.

A new Dell 19-inch (E1914H) monitor runs about $90.00 – 110.00.  I can repair a defective unit in about 20-30 minutes or so, which makes it worthwhile for the client.  When repairing equipment, the cost of labor and parts balanced across the cost of new equipment should be a prime consideration.  Sometimes, it is simply not worth the time to repair something.  In others, like this instance, it makes sense as long as the repair is simple.

This is a Dell E198FPf LCD monitor.  After the initial diagnosis:

Dell E198FPf LCD monitor back lighting problem
Dell E198FPf LCD monitor backlighting problem

The first step is to remove the stand and the four screws behind the stand bracket.

LCD monitor stand removed
LCD monitor stand removed

The hardest thing about this repair is getting the bezel off.  Dell uses a bezel around the monitor face that uses little plastic clips to hold it in place.  To get the bezel off, one needs to press the clips toward the center of the monitor while lifting it up.  It requires the careful application of force.

Dell E198FPf monitor bezel
Dell E198FPf monitor bezel

I start on the bottom and use a small screwdriver in one of the slots to get it started. I start on the bottom because if the plastic gets a little marred, no one will see it when the repair is finished.  Once the first clip is released, then the others and be released by twisting the bezel carefully toward the center of the monitor while lifting.

Monitor bezel removal
LCD monitor bezel removal

Once the bezel is removed, the wiring needs to be disconnected. This consists of the backlight, the data buss, and sometimes the on/off switches, which are mounted on the bezel.

LCD monitor backlight connector
LCD monitor backlight connector
LCD monitor data buss
LCD monitor data buss connector

After all the wiring is removed, there are either two or four screws that hold the power supply to the monitor screen.

LCD monitor power supply bracket  screws
LCD monitor power supply bracket screws

Finally, the power supply board is exposed.  Depending on the model of the monitor, the hex head screws that hold the VGA connector may need to be taken off.  Sometimes not.

LCD monitor power supply
LCD monitor power supply

Removing the screws on the back of the power supply board exposes the capacitors and other components.

LCD monitor bulging capacitors
LCD monitor bulging capacitors

And the culprit is discovered. These two bulging capacitors are causing the LCD monitor backlight power supply shut down making the monitor unusable. The larger one is a 1000 uF 25 volt and the smaller is 680 uF 25 volt. I replaced both with in kind 35 volt units.  I also took the liberty of replacing the rest of the electrolytics on the power supply board (total of five additional capacitors).  While the unit is disassembled, it is far easier to replace all the $0.50 components than to do it one at a time over the next few years as each fails.  This monitor should be good for another 5 years of service at least.  These values vary somewhat from monitor to monitor.  Also, if only repairing one or two monitors, the parts can be obtained at Radio Shack for $1.99 each.

It is a good way to regenerate equipment, even if they are set aside as spares.

The roof is on FIRE!

We don’t need no water, let the… oh, wait… The actual roof is actually on fire you say?

YES: Ahh! Time to run around like crazy people!

Carrier HVAC unit damaged by fire
Carrier HVAC unit damaged by fire

This happened over the weekend at one of our clients in NY. The back story is this; over the last two weeks, the area has received almost three feet of snow. This roof is pitched slightly toward the back of the building. The roofing material is some type of PVC, which is very slippery when wet. Thus, at some point the snow/ice pack shifted towards the back of the building, and it broke the natural gas pipe off where it entered the unit:

Broken gas pipe, HVAC unit 1
Broken gas pipe, HVAC unit 1

The next time the HVAC unit cycled on, there was a giant torch on the roof with flames reportedly eight feet high.  A local firefighter just happened to be driving down the road and spotted the fire, thus likely saving the building from major damage.  The fire department came and cut off the gas and electricity.  The building was evacuated for about 20 minutes while they overhauled and checked for internal fires.

Carrier HVAC unit damaged by fire
Carrier HVAC unit damaged by fire

A second unit suffered the same fate, only with less damage:

Carrier HVAC unit damaged by fire
Carrier HVAC unit damaged by fire

The fire in this unit was contained in the controller area.  Same situation with the gas pipe, only it looks like the pipe was not broken all the way off:

HVAC unit broken gas pipe
HVAC unit broken gas pipe

The other two units are shut off while the gas pipes are dug out of the snowpack and checked for damage. At some point, they will be turned back on so that the heat can be restored to the second-floor sales bullpen. Meanwhile, the salespeople; are complaining.

We threw a tarp over the unit with the cover ripped off because more snow is on the way:

Carrier HVAC unit tarped
Carrier HVAC unit tarped